Well, I'm done for a while.

Discussion pertaining to positive pressure E28s.
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Bill in MN
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Post by Bill in MN »

So much for the track day I had planned on this week, the clutch pack blew on Saturday. While I'm sure the additional power/torque didn't do it any favors, as is with any '86 auto equipped car it's days were numbered. I had started thinking I was going to skate on any tranny issues given the abuse I've put the thing through as of late but it wasn't to be.

I wish I could say it went in a blaze of glory whilst blowing away a Saleen, F40 or some other esteemed vehicle but nope, I was pulling away from a stop sign going to the post office. :(

It's probably going to be off the road for a while so more than likely I'll pull the whole drivetrain and finish the low comp. motor that's going in this winter. Perhaps it was a sign from the boost gods telling me it was time for more :D :D
rundatrack
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Post by rundatrack »

Man sorry to hear that ...

Did you have any issues prior to the turbo?
Jesse
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Post by Jesse »

Just slap some new clutches in and go :cool: .

Well taking care of the stator leak-by too would not be a bad idea since you will have it off in your hand to do the A-clutches anyway :D .
Bill in MN
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Location: The Boonies, Mn
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Post by Bill in MN »

Yeah, now that I think about it there were issues. I passed them off to various reasons, namely the revaned converter changing all of the charactaristics of the tranny. In retrospect it had been telling me for a while. I don't really think it's due to the turbo. It may have accelerated the matter but it would have gone regardless.
stuartinmn
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Post by stuartinmn »

Rats. That means I won't get a ride in it until next year. But, it will be even faster then, right? ;)
Bill in MN
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Post by Bill in MN »

Perhaps not Stuart!!

I conned the local shop into yanking the tranny yesterday. It'll be on my bench this afternoon and with any luck I can rebuild the clutch pack within the next week. I've also located a tranny out of an 89 635 that should not have the clutch pack issue so there is a backup plan. The tranny may be cheap so I may go that route regardless. There's still lots of good driving to be done before the snow flies and if everything goes right it could be back on the road in a couple of weeks!
T_C_D
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Post by T_C_D »

[QUOTE="Bill in MN"]Perhaps not Stuart!!

I conned the local shop into yanking the tranny yesterday. It'll be on my bench this afternoon and with any luck I can rebuild the clutch pack within the next week. I've also located a tranny out of an 89 635 that should not have the clutch pack issue so there is a backup plan. The tranny may be cheap so I may go that route regardless. There's still lots of good driving to be done before the snow flies and if everything goes right it could be back on the road in a couple of weeks![/QUOTE]

Excellent news! You know you need the retrofit kit, correct? It's two tiny washers and a drill bit. BTW, your .8 bar spring is shipping today.
Todd
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