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Posted: Mar 15, 2012 6:20 PM
by turbodan
Never seen one cracked there before. Thats quite odd.

Posted: Mar 15, 2012 7:23 PM
by grey ghost
turbodan wrote:Never seen one cracked there before. Thats quite odd.
I guess I'm lucky the headgasket blew when it did...

Posted: Mar 17, 2012 9:32 PM
by grey ghost
Got the head back on today. But only after seeing that the exhaust manifold bolts on my new head are m8x1.25 and my 745 studs are m10x1.5.
So after going to every part place within 20 miles I decided to drill and tap the holes.
Now I had to find the right bit.
Took two hours to find he right bit and had all 12 holes done just over an hour.
Although we have more daylight, the sun set quick.
I was able to get the intake back on and got 11of12 bolts tight.
That last lower bolt is only finger tight.

I was able to press the head up and in the engine bay with the exhaust manifold and the wastegate perch on it.
That was major.
After scoping it out for about twenty minutes, I went for it and landed it clean........

It sucks that I spent a good portion of the day looking for stuff.
Between looking for studs, looking for the right bit and tapping the holes, I lost about 4 hours today.........

Posted: Mar 18, 2012 6:46 PM
by grey ghost
Well she's alive, again.
It feels weaker.
I didn't get on it, but iits not the same.
Going to recheck the valve adjustment again.
I don't think going from the b35 cam a b34 would make that much difference.

Posted: Mar 18, 2012 6:50 PM
by Nebraska_e28
So you're now using the head I sent you but with a b35 cam? B35 valves?

Posted: Mar 18, 2012 7:07 PM
by grey ghost
Nebraska_e28 wrote:So you're now using the head I sent you but with a b35 cam? B35 valves?
Yes, the head you sent me just as it was. I had I pressure tested and resurfaced.
I knew it would come in handy one day.
So its a straight b34 now.
The other head just had a b35 cam.

Posted: Mar 18, 2012 7:30 PM
by turbodan
I hope you turned the boost down. It should feel weaker.

Posted: Mar 18, 2012 7:47 PM
by grey ghost
turbodan wrote:I hope you turned the boost down. It should feel weaker.
Boost is back to 10psi.
The throttle pedal seems a little stiff.
I'll have to diagnose that in the morning.

Posted: Mar 19, 2012 10:54 PM
by grey ghost
So if I compare the way the car is running now at 10psi to were it was before and 10psi, I have to say its a straight pig.
Its slow, spool up is much slower.
I don't know what the hell is going on.
Whats the chance its my valve adjustment. I'm no master but that's one thing I feel I can do well.
I did .009 on the cam side. I does sound a little quieter but I can still hear the mechanics.
There's no way its this sluggish just because of the different cam b34 now, b35 then.
The car has no spunk anymore.

Posted: Mar 19, 2012 11:03 PM
by Kyle in NO
Cam timing is off.

Posted: Mar 19, 2012 11:08 PM
by grey ghost
Kyle in NO wrote:Cam timing is off.
Dude, you know my experience with timing, and while you may be correct, I check and check and check 7 more times before I buttoned it back up.
I hear that one tooth is not too bad, so I would have to be off by at least two teeth, and I don't think thats so....
But I will check.

Posted: Mar 20, 2012 5:19 PM
by grey ghost
Timing was off by a tooth, but it still feels sluggish.
I can't even hear the turbo spool up.
Its completely different....... Sucks
I'll recheck the valve adjustment in the morning..

Any other suggestions??

Posted: Mar 20, 2012 6:21 PM
by turbodan
If your AFR hasn't changed and you have good compression I don't know what else to tell you. A compression test will indicate an issue with the valve adjustment or valve sealing. It could be a boost leak or a leaky exhaust manifold as well.

You turned the boost down to 10 psi. It might just be in your head since you were used to running more. If the engine is making a certain amount of boost at a certain AFR its going to be making a certain amount of power assuming nothing has happened to affect the ignition timing. IIRC you're running Motronic with a TCD chip, so I can't imagine what could be pulling timing.

Posted: Mar 20, 2012 7:05 PM
by grey ghost
turbodan wrote:If your AFR hasn't changed and you have good compression I don't know what else to tell you. A compression test will indicate an issue with the valve adjustment or valve sealing. It could be a boost leak or a leaky exhaust manifold as well.

You turned the boost down to 10 psi. It might just be in your head since you were used to running more. If the engine is making a certain amount of boost at a certain AFR its going to be making a certain amount of power assuming nothing has happened to affect the ignition timing. IIRC you're running Motronic with a TCD chip, so I can't imagine what could be pulling timing.
I just had the head pressure tested and it check out perfectly.
AFR's have not changed.
The boost gauge goes to 10psi, but its like it does want to.
It feels like I'm pulling an anchor.

I can clearly remember the boost spooling even when I was at 10psi. That's the reason I stopped listening to the radio.

Seriously, its slower off the line now than it was when it was a stock 535is.
Something is wrong....

I'll check the valves lash tomorrow, again. I have to grab my compression testing goodies from storage, I knew there was something else I needed to get the last time I was there.....

Posted: Mar 20, 2012 7:20 PM
by T_C_D
grey ghost wrote:
turbodan wrote:If your AFR hasn't changed and you have good compression I don't know what else to tell you. A compression test will indicate an issue with the valve adjustment or valve sealing. It could be a boost leak or a leaky exhaust manifold as well.

You turned the boost down to 10 psi. It might just be in your head since you were used to running more. If the engine is making a certain amount of boost at a certain AFR its going to be making a certain amount of power assuming nothing has happened to affect the ignition timing. IIRC you're running Motronic with a TCD chip, so I can't imagine what could be pulling timing.
I just had the head pressure tested and it check out perfectly.
AFR's have not changed.
The boost gauge goes to 10psi, but its like it does want to.
It feels like I'm pulling an anchor.

I can clearly remember the boost spooling even when I was at 10psi. That's the reason I stopped listening to the radio.

Seriously, its slower off the line now than it was when it was a stock 535is.
Something is wrong....

I'll check the valves lash tomorrow, again. I have to grab my compression testing goodies from storage, I knew there was something else I needed to get the last time I was there.....
Wastegate stuck open?

Posted: Mar 20, 2012 7:27 PM
by grey ghost
T_C_D wrote:
grey ghost wrote:
turbodan wrote:If your AFR hasn't changed and you have good compression I don't know what else to tell you. A compression test will indicate an issue with the valve adjustment or valve sealing. It could be a boost leak or a leaky exhaust manifold as well.

You turned the boost down to 10 psi. It might just be in your head since you were used to running more. If the engine is making a certain amount of boost at a certain AFR its going to be making a certain amount of power assuming nothing has happened to affect the ignition timing. IIRC you're running Motronic with a TCD chip, so I can't imagine what could be pulling timing.
I just had the head pressure tested and it check out perfectly.
AFR's have not changed.
The boost gauge goes to 10psi, but its like it does want to.
It feels like I'm pulling an anchor.

I can clearly remember the boost spooling even when I was at 10psi. That's the reason I stopped listening to the radio.

Seriously, its slower off the line now than it was when it was a stock 535is.
Something is wrong....

I'll check the valves lash tomorrow, again. I have to grab my compression testing goodies from storage, I knew there was something else I needed to get the last time I was there.....
Wastegate stuck open?
I thought of that but I also thought that I wouldn't get any boost if it was struck open.
That would definitely explain the lack of spool sound.

Posted: Mar 20, 2012 7:48 PM
by turbodan
Maybe pull the compressor inlet piping off and take a look at the turbo. Check shaft play and wheel condition.

Posted: Mar 20, 2012 8:03 PM
by grey ghost
turbodan wrote:Maybe pull the compressor inlet piping off and take a look at the turbo. Check shaft play and wheel condition.
Thanks, I'll take a look tomorrow...

Whats weird about the whole thing is that the idle is rather smooth, more so now than ever..
I guess the b34 cam is helping that..

Posted: Mar 21, 2012 10:06 PM
by clongo
How did you go about running less boost? Didn't you crush your wastegate until you were hitting like 18-20psi?

Posted: Mar 21, 2012 10:10 PM
by grey ghost
clongo wrote:How did you go about running less boost? Didn't you crush your wastegate until you were hitting like 18-20psi?
Yeah, I crushed it.
But regardless, you get nothing additional until you block the signal line.
So I reconnected the signal line and I'm back to 10psi.

Posted: Aug 28, 2012 8:01 PM
by shocka
Any updates?

Posted: Aug 28, 2012 9:34 PM
by grey ghost
shocka wrote:Any updates?
Yeah:

Overboosted and cracked the head, blew the hg.
replaced the head with a stock head, 12psi, probably still too much.
waiting to find an upgraded k27 for sale.
I would love to buy a new one from TCD, but its a little too steep for me right now.
Car is running pretty good.
Once I score an upgraded k27, I'll go ahead and build another head, maybe with a bigger cam, or just the b35 like before.
I also plan on a FMIC and maybe moving the throttle body to the other side of the intake.

All dreams at the moment......

Posted: Aug 28, 2012 11:34 PM
by Brad D.
What did it overboost to? Glad it's up and running.

Posted: Aug 29, 2012 6:34 AM
by grey ghost
Brad D. wrote:What did it overboost to? Glad it's up and running.
After I compressed the wg and blocked the signal line, it would go right to 20psi with the quickness.
In my ignorance and in amazement at how fast it was, I played with it for a while. It was major fun while it lasted.

The fat girl

Posted: Aug 29, 2012 7:17 AM
by mpowertech
Maybe we can nudge Todd to do a two guy group buy for us. I need to find some shit to sell :heehee:
With a FMIC the fat girl is going to love Boston in the winter!
Hope you're well!

Re: The fat girl

Posted: Aug 29, 2012 10:07 AM
by grey ghost
mpowertech wrote:Maybe we can nudge Todd to do a two guy group buy for us. I need to find some shit to sell :heehee:
With a FMIC the fat girl is going to love Boston in the winter!
Hope you're well!
Yeah, my car loves the cool weather, I can feel it already with these 50degree mornings up here in western MA.

As for Todd, I'm not sure there's wiggle room in there.... and if there is, I'm sure its still a little steep......
But I hear the upgraded k27 is extremely nice....... do want

I've already picked out a big whopping FMIC, need to take the front end apart and do some measuring...
There's goingt o be some fab going on down there....

Posted: Sep 13, 2012 9:49 PM
by grey ghost
So I happened along an S3.46 last weekend and I'm debating on installing or selling......
I'm running aS2.93 now....

To install, or not to install, that is the question....

Posted: Sep 14, 2012 12:12 PM
by Shadow
that will sure fix your slowness problem.

Posted: Mar 10, 2013 10:30 PM
by grey ghost
Blew her up again. Oh well. Time for a cometic mls gasket. b35 cam is going back in. I may go with a air to water intercooler.

Posted: Mar 10, 2013 10:48 PM
by turbodan
Why A/W? Were you having trouble with intake air temps?