Got bored at work, wrote up my life story
Posted: Oct 04, 2024 7:28 PM
Sometime in 2004 I found my first e28. This is a four door sedan made by BMW from 1982 through 1988. The common models available in the US had either a 2.7, 3.2, or 3.4 liter inline six cylinder engine. This one was listed for sale on the Roadfly message board in the classified section. This was a nationwide forum, but this car happened to be located only a few miles away from me. It was a 1985 528e in Alpine White, with a pearl-beige interior and a 5-speed manual transmission. The owner listed it in non-running condition, so upon paying $1300 for it we towed it home. From a storage unit off of Highway 528, we pulled it with my Dad’s Nissan pickup and a tow strap all the way back to the house. With some basic troubleshooting it was soon determined that something had gone wrong in cylinder number 5, as the spark plug showed substantial physical damage that was indicative of ingestion of some sort of foreign debris. This required a nearly full disassembly of the engine to inspect the cylinder head and bottom end. The head showed only superficial damage, so with not much more than the bare engine block left in the car, we began reassembly. One piston was replaced, the bottom end was buttoned up, the cylinder head was reinstalled as well as the manifolds, wiring and fuel system connections.
Upon initial start-up, the oil pump did not prime and the engine ran for nearly a minute with no oil pressure. Once we realized that this situation was not going to remedy itself, the oil pan was removed, the oil pump inspected, and the pan reinstalled. The second time was the charm, as the oil pump began to pump oil and the engine ran once again. The car had somewhere in the vicinity of a quarter million miles on it, though most of them were done on the highway. Overall, it was in good condition cosmetically but it was one of the slowest cars on the road. This model was never intended to generate excitement, it was mildly tuned from the factory and produced a very modest 121 horsepower at the crank, at sea level. At my altitude, around 5500 feet above sea level, it was producing about 102 horsepower and perhaps 85 of those were making it to the rear wheels.
For the sake of comparison, I currently own a 2002 Yamaha FZ1, a 1000cc sport touring motorcycle that makes 130 horsepower at the rear wheel, and probably about 107 at my altitude. Comparing these two in terms of their power to weight ratio, the e28 carries 35 pounds for each one of its horsepower and the FZ1 has less than five. On the road, this means one of these vehicles will run a standing start quarter mile in 10.62 seconds at 130 miles and hour, and the other clears the quarter in about 19 seconds with a trap speed of about 80 miles per hour. Zero to sixty times are another common benchmark for performance, and here again the FZ1 gets the job done in under three seconds while the 1985 four door sedan will struggle to get to 60 in less than ten. In the simplest terms, this car was a slug.
As I imagine is typical, the ordinary young man has a strong interest in making his car go faster and I was no exception. I had been riding bicycles since I was very young and loved going fast, riding wheelies, and hitting jumps. I began riding motorcycles when I was about ten years old, and those went even faster still. I rode motocross at a competitive level into my high school years and was accustomed to high performance machines. The car did not fit in with my sensation seeking nature, and I very quickly began looking into what could be done to improve its performance. People on the internet suggested a performance chip for the computer and a lower final drive ratio, giving the engine more mechanical advantage over the weight of the vehicle. These modifications were done without delay, but the car was still dreadfully slow. One of the worst things I have ever done to a car followed shortly thereafter, which was the removal of the original exhaust system and the installation of glass-pack mufflers. I never liked the sound, which was loud and awful to an extent beyond my ability to describe, but I had hoped to increase performance with a minimally restrictive exhaust system.
The results were not outstanding. If the car was any faster it was only by an imperceptible amount. The noise was horrendous, which reverberated and droned inside the cabin in a way that may have sounded even worse than it did to those outside the car. Not to be deterred, my attempts at finding horsepower continued. I installed a larger air flow meter, larger fuel injectors, a larger throttle body. None of this made any difference, other than to make the car less fuel efficient and less reliable. Eventually, I decided it was time to do some more substantial engine work. I found a camshaft from an M20B25 and a cylinder head from a 323i, both being different variations of this engine in a more performance-oriented state of tune. This camshaft and cylinder head were installed and the engine actually responded with an increase in power. Still, not a fast car by any means but I was moving in the right direction.
The next step forward was significant but quite difficult. The original engine management system was not calibrated to work with anything other than the standard M20B27 engine. Upon installation of the 2.5 liter cam, the engine dynamics had been changed significantly and the computer was now a significant obstacle to progress. I made a feeble attempt to explore EPROM tuning, which I had no chance of accomplishing anything with. What I needed to do was install the 2.5 liter engine management system, which meant re-wiring a harness from a later 3 series and splicing it into a 5 series engine compartment and the existing wiring around it’s periphery. Many of the sensors were different, so these needed to be changed over as well.
Not to be deterred, I began scouring through the BMW ETM. This is the electrical troubleshooting manual which contains comprehensive wiring diagrams for both the donor car and my 5 series. The main obstacle was the C101 junction at the fuse box, through which many of the critical connections were carried. About 16 wires needed to be spliced, and since the connector was a different type on the 3 series harness the e28 connector had to be carefully grafted on. Various other changes were required, mostly wiring extensions, but the work was soon completed. With the homemade wiring harness and all of the correct sensors and switches installed, the car did not start. I was disappointed, but not too surprised.
Looking back over the ETM, I checked all of my work and verified all of the connections. Everything I had done was correct, but the car did not start.
I considered this situation over the following days. Looking back over the C101 connections, I realized that there was nothing here that connects the DME to the ignition switch. This seemed like it would be necessary. How would the ignition key turn the engine off if there were no connection between the two? I looked at that section of the ETM and quickly discovered the culprit, a few wires going through a separate and not terribly important looking connector in the vicinity of the glovebox. This C104 junction carried the very important start/run signal to the computer, as well as the tachometer signal and a fuel consumption information to the instrument cluster.
A few quick splices here and the engine started immediately. The new engine management system was a vast improvement over the previous iteration. The improved idle control system was immediately apparent, and it also had advanced adaptive capabilities to adjust fueling for maximum efficiency. Best of all, the fuel and ignition mapping were suited to work with the camshaft and intake manifold I had previously installed. The car was running quite a bit better by this point, although still unacceptably loud.
The next few steps were more of the same. I installed some low quality “shorty” headers. I ordered a reground camshaft with more lift and duration. I sourced an intake manifold from a 323i on German eBay and had it shipped in. I found a chip from an Alpina C2 2.7, which was a German builder who specialized in tuning these cars. There couldn’t have been more than a few hundred of these made originally, but I found a chip out of one of those and plugged it into my DME. It provided more advanced ignition timing and a fuel map suited for a more aggressive camshaft profile.
At one point during the summer of 2006 while I was working at BMW, one of my co-workers informed me that his dental hygienist mentioned that she had an old BMW she was looking to get rid of. Vinny knew this was right up my alley, so he passed her information along and I got in touch. The car was located in a barn in Tome, NM and had been sitting for a very long time. The owner indicated that there was a problem with the alternator, but overall the car was a viable candidate. Being a 1988, it came with a number of desirable parts, including a factory installed version of the fuel injection system I had just painstakingly wired into my ’85. The price was $500, and I was shortly on my way back down to get it. The plan was to drive down in my ’85, put the good battery from my car into the ’88, the dead battery from the ’88 into the ’85, start the ’88 with the good battery and dead alternator, jump start the ’85 with the good alternator and dead battery, and drive both cars home about 45 miles before the battery in the ’88 ran down. The drive was about an hour, 45 miles distance. My buddy Brain soon discovered that the brakes didn’t work very well and nearly rolled out in front of a passing truck on highway 47. After that though, we had no issues. Both cars made it home and my second e28 project had begun.
Fortunately for myself, the neighbors, and the rest of Rio Rancho, this ‘88 had a factory dual exhaust system which was suitable for the level of horsepower I was making. Some welding was required to repair the center resonator but the system in general was solid. The glasspacks were unceremoniously shit-canned and the complete, stock ‘88 exhaust system was installed on my ‘85. The car seemed to run better than ever, while being quiet and pleasant to drive. Meanwhile, the ’88 was in the process of being comprehensively stripped down. The interior was ruined with rodent activity, so it was gutted and new carpet, seats, and dashboard parts were ordered. The engine and transmission were removed for a rebuild. This car was originally an automatic which I had no plans on retaining, so the process of converting the driveline to a manual transmission was started. This was quite easy with the engine and everything else out of the way.
At this point with the original Alpine White ’85, I had essentially reached the end of what was achievable within the limitations of this engine’s displacement and design characteristics. There were no stones left unturned, no other parts left to try. The only ways to make more power were to increase the size of the engine or spin it at higher RPM. There are practical limitations to both approaches. For the ’88, a new plan was devised using forced induction to break out of the confines of the 2.7 liter, single overhead cam architecture. Forced induction utilizes a compressor, either a belt driven supercharger or exhaust gas driven turbocharger, to supply more densely compressed air in high volume to the engine. This pushes more air mass into the existing engine and correspondingly more oxygen into the combustion chambers. Atmospheric pressure at my altitude is about 12.2 pounds per square inch. If I were to add 12.2 pounds of boost with a turbocharger, it should in theory double the amount of power the engine produces.
In practice, it doesn’t quite work out that well. The turbocharger presents a restriction in the path of exhaust gases trying to egress from the combustion chambers. This suppresses volumetric efficiency by leaving excessive residual pressure behind after the piston attempts to “blow down” the cylinder on the exhaust stroke. This residual gas remains behind in the cylinder and occupies a certain volume that cannot be filled by fresh fuel and air on the following intake stroke. If a belt driven supercharger is used, the power to drive the compressor is subtracted directly from the crankshaft. Neither approach is perfectly efficient, but both will make power.
I decided a turbocharger was the way to go. I spent countless hours reading everything available on the subject. I pored over technical information available from turbocharger manufacturers. Honeywell Garrett had an excellent website with comprehensive information regarding compressor characteristics and equations that could be used to determine what kind of air mass would be required by any given engine at any given boost level. My calculations determined that a GT2560R compressor would likely be suitable for my engine at my elevation, so I bought one, part number 466541-4. Originally, I didn’t plan on high boost levels or outrageous performance, so this turbocharger being capable of about 300 horsepower was the ideal choice.
The first problem was, how to install this device on a BMW M20 engine? This engine was never designed for turbocharging and all I have available are the various exhaust manifolds BMW manufactured for this engine. A turbocharger is generally installed close to the engine, though it can be installed practically anywhere you can fit it. They have been installed in place of rear mufflers, sticking out of hoods, inside passenger compartments, and in spare tire wells just to name a few options. I considered a rear mounted system for the sake of room, but I didn’t want to deal with feeding and returning pressurized oil to and from the back of the car. This Garrett turbo was water cooled as well, so it would also require a pair of coolant hoses running to and from where it was located. The oil return would require an electric pump, which is a potential point of failure along with the many feet of plumbing to carry these vital fluids.
After some research and consideration, I decided a conventional installation in the engine compartment was the way to go. BMW had made a diesel version of the engine with a turbocharger, and the manifold could be modified to fit the gas engine. I ordered a manifold and began work on modifying it. The manifold itself was close enough to work, only requiring a few hours of drilling, grinding and notching to fit the stud pattern on the gas engine. I found the cross-sectional area of the collector to be smaller than I liked, so I ground this out until it was significantly larger than the turbine that it fed into.
The ’85 528 was still on daily driver duty while the ’88 project progressed. By this time, it had accrued more than 314 thousand miles, the most recent of which under my ownership had seen a lifetime worth of what some might consider abuse. It was modified and making more power than ever, and being driven in a way that I’m certain it had not been accustomed to. Eventually, this would come to an end. On my way to work one morning, it began to emit a rapid, metallic, cyclical tapping noise at moderate RPM under light load. This was the sound of rod knock, which occurs when a connecting rod bearing can bear no more. The bearing had “spun” inside of the connecting rod and had opened up too great a clearance for the hydrodynamic film to carry and cushion the reciprocating load. The engine was finished. I made it to work, then back home again as carefully as possible, and the car never drove again after that.
This situation was problematic, I still had to get to work. I did have some vacation time so I used that to put in some work on the ’88. The interior had been refurbished and only the driveline remained to be addressed. I already had that engine stripped down, cleaned up, and I had parts on hand to rebuild it from a bare block. Starting with the main bearing shells, then the crankshaft, then the main bearing caps, then the rods and pistons. The front timing cover, rear main seal carrier, the oil pump and oil pan. The short block was done in an afternoon. The cylinder head had been assembled previously and was ready to install. The ’88 had a different cylinder head with larger valves and improved combustion chambers, suited to fit the hemispherical dish-in-a-dome pistons. A significant improvement over the ’85 engine, even before forced induction.
Over the course of that week, I finished assembly of the engine, installed the engine in the car, installed the transmission, driveshaft, wiring harness, reinstalled the ’88 exhaust from the deceased ’85 and got the car running before the weekend. This was a car built from a gutted, empty shell. It had its own sort of new car smell. It had a new interior, with seats I had upholstered, new carpet and new trim. The scent of the simple green I used to clean the rodent urine from the sheet metal stampings of the floor may have been faintly present. One of the last things I needed to do was bleed the brakes, which were still full of original 1988 vintage DOT 3 fluid. It was semi congealed into a lumpy, slimy broth. No wonder the brakes didn’t work.
At this point, it was on the road but not yet turbocharged. The timeline of the project had been disrupted by the untimely mechanical failure of the ’85. In any case, it was on the road and it ran beautifully. The engine was new, cylinder and valve leakage was near zero. The valvetrain was new, the camshaft was new, everything that mileage and use subjects to wear was fresh and in perfect condition. Power balance across all six cylinders was optimal. It delivered strong, smooth power over a broad range. This was a satisfactory result for the substantial work that had gone into the ’88 up to this point. With my transportation needs met, work on the turbo project continued.
I had begun to accumulate a sizable collection of spare engine parts, including a cylinder head I used to test fitment and mockup the turbo and manifold. The GT2560R used a larger compressor than BMW had fitted on the diesel engine, which would not clear the valve cover when installed. A simple but inelegant solution to this was a stack of at least seven or eight T25 flanges between the manifold and turbocharger, raising the turbo high enough to clear the cylinder head and bolt everything together. I ran this setup for probably a year and a half, having to periodically tighten the very long bolts used to hold the large stack of flanges together. Exhaust leaks were constant but with the volume of flow through the engine it had little effect on the operation of the turbocharger.
Next up was plumbing. Turbochargers draw atmosphere through a short inlet system to filter undesirable particles and deliver this under pressure through a length of plumbing. This reaches from where the turbo was located all the way to where the throttle body admits air into the intake manifold. Any self-respecting builder will certainly include an intercooler to get rid of the heat generated by the compression of the air through the turbocharger, which lengthens and further complicates the plumbing. I started with a small front mounted air to air intercooler, located below the air conditioning condenser under the front bumper. I was still considering trying to retain the functionality of the air conditioner at this point, so a certain trade off was required at the expense of intercooling.
The ’88 was now the daily driver, but I was able to begin to fabricate and assemble the plumbing in a piecemeal manner. The intercooler was installed on improvised brackets and the plumbing worked outward in both directions. The compressor outlet was on the passenger side of the engine compartment and the plumbing was constructed to feed downward and curve through the bodywork in a horseshoe shape around each side, where it connected to the intercooler in front. The throttle body was on the driver’s side, where the plumbing came up just inside the frame rail and fed into the air flow meter, which the computer uses to determine the load on the engine.
This was probably the most significant obstacle to turbocharging this engine. The turbo can supply a massive amount of air mass to the engine, however the stoichiometry of combustion requires a correspondingly large amount of fuel to be delivered to maintain an appropriate air/fuel ratio. The fuel injection system was never designed to work with anything other than atmosphere, so this required some engineering. At the time in 2006, options were limited. The best solution at the time was a rising rate fuel pressure regulator. This simple device references fuel pressure to boost pressure, and scales up fuel pressure at an adjustable rate of gain to deliver enrichment under boost. The computer does not see the boost or any change in load and the engine still displaces 2.7 liters. The RRFPR simply overrides the standard fuel pressure regulator when boost pressure is generated. The computer fires the fuel injectors for the exact same duration that it would ordinarily, but with the increased fuel pressure additional fuel is delivered.
This completely resolves the enrichment issue, but doesn’t completely address the obstacle posed by the fuel injection system. The other factor must be addressed is ignition timing, which is advanced at lower loads and pulled back at higher loads. The original computer handles this assuming maximum load is at atmospheric pressure. With forced induction, maximum load is determined by the maximum boost pressure and ignition timing should be scaled downward further as boost increases. If the air fuel ratio or ignition timing is not carefully adjusted, abnormal combustion occurs known as “detonation” which is a spontaneous, powerful and rapid ignition of mixture inside the combustion chamber. This phenomenon is very destructive and is the most common cause of engine damage in high performance engines, especially those using forced induction.
Fortunately in a way, and unbeknownst to me at the time, my intercooler was significantly undersized. It was unable to control charge air temperatures effectively, so the air flow meter was seeing significantly elevated air intake temperatures. The original computer responds to this by pulling back ignition timing to avoid detonation, which is exactly what was needed to save my bacon. I’m not sure to what extent this was beneficial overall, as these same elevated air intake temperatures contribute to detonation as this heat enters the combustion chamber and exacerbates the adiabatic heating that occurs during the compression stroke.
In any case, with the fuel enrichment handled and a certain amount of indifference toward my inability to address ignition timing, I moved on with the project. The turbocharger and exhaust manifold were ready, I had flanges, bends and tubing to fabricate a new exhaust system. I had the intake plumbing essentially competed. I had routed coolant from the original throttle body heater circuit to the turbocharger. I tapped into the clean, pressurized supply of oil available at the oil cooler adapter and installed a fitting here to supply the turbocharger. The oil return was plugged haphazardly into the oil pan and sealed with the finest quality high strength, steel reinforced epoxy.
In spring 2007, the ’88 was ready for boost. The installation did not require vacation time as all of the loose ends and potential hang-ups had been sorted out in advance. The manifold had been test fitted, the plumbing had been fabricated and was already almost completely installed before I installed the business end of the system. I would still need to sort out the rate of gain on the RRFPR to dial in the fueling, but this was a simple device with few adjustments. Cautiously at first, the original turbo 528e hit the road. The tuning was simple enough, I had previously spent many hours adjusting carburetors on the dirt bikes to fine tune fuel mixtures. This experience translated well to the turbo car. I started with excessively rich, or fuel heavy air fuel mixtures. As I leaned the mixture out, the car stopped breaking up and misfiring and began making what felt like a ridiculous amount of horsepower.
At that boost level, I would estimate the car was making about 200 rear wheel horsepower. At the crank, close to 240. This car was quick even at 7 psi. For this altitude, anything without a turbo on it is paying a roughly 20% penalty with the reduced air density. A stock LS1 in a Camaro SS or Trans AM WS6 was making 300 horsepower at the crank, at sea level. In Rio Rancho at the rear wheels? Maybe 205. I recall a specific instance where I lined up with one of those LS-equipped Pontiacs, and we both opened it up when the light turned green. Though both cars were accelerating rapidly, we were completely stationary relative to one another. Despite the vastly different powertrains and 20+ year difference between these cars, the different gear ratios and torque curves, we were accelerating at exactly the same rate. I think we let off at about 100, which was fortunate as there was a police officer sitting in a Target parking lot off to the side, perhaps another quarter mile down the road. We would have been going more than triple the posted limit by that point, and doing so while street racing. That could have been a bad night, but was the first of many such close calls.
I would have loved to talk to the guy in the Pontiac. I couldn’t believe I hung with a car like that, and I’m sure they were just as surprised as I was. This was the most awesome thing about that e28. Dragged out of a barn, covered in rodent excrement. Resurrected, at least mechanically, and modified to produce enough power to stand toe to toe with the latest iteration of GM’s high performance 5.7 liter V8. Though the interior was nice, the paint and body on the ’88 was not on the same level as the ’85. Even when new, it was painted a butt-ugly metallic brown. Nerzbraun, if I remember correctly, which translates to “Mink Brown”. The paint was faded and the clear coat had begun to peel, so it wasn’t much to look at in 2007. Worst of all, the car had been hit and damaged in a rear end accident shortly after it was returned to the road. The damage had affected the right rear quarter panel and broken the rear bumper in half. This pissed me off severely but it didn’t look too bad once I had replaced the taillight. The car had been paid out as a total loss, so I had more money for turbo parts. This disguise added to the shock and dismay of it’s victims. You would never see it coming, and it was a serious contender.
Shortly after the system was completed, the ’88 went to the dragstrip for a sort of performance evaluation. This provides a substantive basis for comparison, the sum of all factors. Some aspect of this is left to the ability of the driver but for the most part, the quarter mile run provides a very good test. Launching this car was difficult, even with relatively mild amounts of horsepower. This was the furthest thing from this vehicle’s intended purpose, and the power output of the original engine had been more than doubled. Despite uniformly poor results in the first 60 feet, during the period between not moving and moving, the car covered the distance in very close to 14 seconds flat. Better launches and a lower 60 foot time would have provided better ET’s, but a 14 flat is nothing to sneeze at. Trap speeds were around 100 miles an hour, which roughly corresponds to the elapsed time.
The thrill and euphoria of these things is unfortunately short lived. Given a few weeks of excitement, the newfound performance became familiar and increasingly ordinary. Still a young man, always looking for more, I began exploring the possibility of turning the boost up beyond the original .5 bar allowed by the wastegate actuator. The system was already marginal in many ways, and I bumped against these limitations as soon as I tried to push more boost. The original computer knew nothing of the hot rod shenanigans that it was involved with, and was increasingly unsuitable for boost as it crept higher. I found a custom chip with moderated ignition timing through Todd at TCD, a supplier who had recently brought legitimate turbo systems to market for e28’s. This got me to 11 psi, which made the car go faster still. I had to resort to zip ties and duct tape between the air flow meter and throttle body though, as the original rubber boot was never designed to hold even a strong vacuum, let alone 11 pounds of boost. Fuel pressure was reaching levels more than double what the system was intended to run, which was soon going to require more fundamental changes.
This was about when the car went to the dyno for the first time. Quoting myself from forum posts of the period, I was running 11 psi and the car made 230 rear wheel horsepower and 266 foot-pounds of torque. This would perform comparably to a contemporary BMW M3, whose S54B32 engine produced 333 horsepower. At my elevation, 333 crank horsepower translates to 227 at the wheels. And my e28 was lighter. My only gripe at the time was the relative lack of top end power, the dyno curve began to drop excessively as revs passed 5500 RPM. Peak horsepower was lower than would be expected for this engine configuration, so something was suppressing the last third of the power curve. In hindsight, I think this can be attributed to the insufficient intercooling and rapidly climbing intake air temps. Not only does this elevate the probability of detonation, the hot boost is less dense than it could be, as the overall air mass delivered for a given volume of air is reduced.
I think the highest I ever went with the original system was 14 psi, and this was more than the original clutch could handle. I had to turn it back down immediately and start shopping for a stronger clutch. Todd at TCD had a solution for me for a few hundred dollars. This was an organic disc with a special pressure plate designed to generate lots of clamping force. Designed to hold almost 400 foot-pounds of torque. That seemed sufficient for any prospective boost levels, so I ordered one up.
The next step for power was a bigger turbo and standalone fuel injection. I was not at all concerned about a bigger turbocharger, this is a bolt on affair. My hypothesis was that the GT2560R was restrictive on the turbine side, which presents a choke point for the exhaust gases on their way out from the combustion chamber. Every pound of air that goes through the engine has to squeeze through this opening in the turbine housing that was approximately the size of a large grape. 230 rear wheel horsepower requires about 23 pounds of air per minute, which is a lot of air. A larger turbine would trade off some of the response and raise the boost threshold, which is the RPM which the turbo fully spools and makes significant boost. Regardless, this was the next step, so the turbo was ordered, a Garrett GT2871R .86, part number 472560-15. Part of the appeal of the GT2560R was that it shared almost all of it’s design features with a family of other turbochargers. Garrett described these as “outline interchangeable”, meaning I could bolt on a larger unit without having to weld on new flanges or change plumbing.
The real battle was shaping up for fuel injection. My ability to work around the limitations of Bosch Motronic was at its end. I had done all I could but it was simply no longer possible to make any more power without an unacceptable risk of engine damage. The solution was a product called Megasquirt, a standalone computer that replaces the original engine management computer and offers full control over every parameter of the engine’s operation. Tuning can be performed while you drive with a laptop computer. This sounds great, but it also means that you are responsible for configuring and tuning every single parameter of the engine’s operation. I wanted more power though, so I found a guy in the e28 community who was building these MS2 kits into the original Bosch Motronic boxes. This allows a plug and play functionality, which retained the ability to plug the original computer back in if need arose and I had to get the car home.
At the time, this was the most significant challenge of the project. This was far above and beyond fabrication and designing a layout. I had read a great deal about tuning, and I had a lot of experience with carbs on two stroke engines. I had no experience building three dimensional maps for fuel and ignition timing though, let alone tuning acceleration enrichments, cranking pulsewidth, configuring ignition settings or any of the other 100+ variables that I was now trying to sort out. It could be compared to teaching someone how to put on shoes, stand up, walk, run, jump, then compete at an Olympic level. This is a process that stretches into the hundreds of hours.
The good news in that the car did eventually get going on standalone, and the new turbo did make more power. Standalone injection offered many advantages once the initial period of configuration hell had been successfully navigated. I now had the ability to record datalogs containing a record of every sensor input and every output by the standalone computer. I had shortly discovered how severely undersized my intercooler was by observing the intake air temperature under boost. It climbed as rapidly as RPM, reaching levels that would rapidly defrost a breakfast sandwich. I immediately ordered another intercooler to install in series with the original. The internet said it couldn’t be done, that pressure drop would be too great and it would be horribly inefficient. I did it anyway. Pressure drop was not significantly greater than it was with the single front mounted intercooler and the intake air temps were within twenty degrees of ambient. A significant improvement in both performance and reliability.
The next trip to the dragstrip was later that summer. On this night, with more boost provided by the larger turbocharger and supported by the standalone fuel injection, the car was running 13 second quarter mile times at 108 miles an hour. Launching was still not great, and this was the only thing holding the car back from breaking into the 12 second category. I had to settle for a best ET of 13.01 at 108 miles an hour. The car got off the line better on the street. The surface at the dragstrip was a nearly smooth type of pavement with a coating of rubber laid down on top. With the right type of tire, this generates enough traction to destroy driveline parts and tear subframe and differential mounts right out of the unibody. With the type of tires I was running, I could only produce wheelspin at best. I rarely drove at the dragstrip and drag radials would almost certainly require a substantial reinforcement of the rear suspension, so this was fine with me.
The next trip to the dyno was in the fall of 2007, and the car made 300 rear wheel horsepower and 360 foot-pounds of torque. Would compare well on the streets of Albuquerque to a non-turbo engine that makes 450 crank horsepower at sea level. It did in fact compare well to a stock BMW 335i, the new twin turbo 3 series introduced in 2007. Another member of a local car forum had one of those and was left behind by bus-lengths while going head to head with the e28. Video of this evening still exists in the hallowed halls of YouTube. That was a fun night, and I engaged in this sort of high risk activity on a frequent basis.
One instance in which I wasn’t so lucky occurred on a lunch break, likely on my way to Arby’s for a three for five deal. I had come down Second Street and gotten on eastbound Paseo Del Norte, and seeing a clear road ahead for at least a half mile I put the hammer down. The turbo spooled up in third gear and the traffic that was once close behind diminished to distant specks in the rearview mirror. I had not checked my mirrors closely enough though, as there was a Bernalillo County Sherriff among that group of cars. Third gear would hit 120 and I’m pretty sure it did before I began coasting down toward Jefferson. About the time I got off the power, I observed the red and blue lights catching up from behind, and I pulled over on Jefferson for what was certain to be an unpleasant experience.
Upon initial start-up, the oil pump did not prime and the engine ran for nearly a minute with no oil pressure. Once we realized that this situation was not going to remedy itself, the oil pan was removed, the oil pump inspected, and the pan reinstalled. The second time was the charm, as the oil pump began to pump oil and the engine ran once again. The car had somewhere in the vicinity of a quarter million miles on it, though most of them were done on the highway. Overall, it was in good condition cosmetically but it was one of the slowest cars on the road. This model was never intended to generate excitement, it was mildly tuned from the factory and produced a very modest 121 horsepower at the crank, at sea level. At my altitude, around 5500 feet above sea level, it was producing about 102 horsepower and perhaps 85 of those were making it to the rear wheels.
For the sake of comparison, I currently own a 2002 Yamaha FZ1, a 1000cc sport touring motorcycle that makes 130 horsepower at the rear wheel, and probably about 107 at my altitude. Comparing these two in terms of their power to weight ratio, the e28 carries 35 pounds for each one of its horsepower and the FZ1 has less than five. On the road, this means one of these vehicles will run a standing start quarter mile in 10.62 seconds at 130 miles and hour, and the other clears the quarter in about 19 seconds with a trap speed of about 80 miles per hour. Zero to sixty times are another common benchmark for performance, and here again the FZ1 gets the job done in under three seconds while the 1985 four door sedan will struggle to get to 60 in less than ten. In the simplest terms, this car was a slug.
As I imagine is typical, the ordinary young man has a strong interest in making his car go faster and I was no exception. I had been riding bicycles since I was very young and loved going fast, riding wheelies, and hitting jumps. I began riding motorcycles when I was about ten years old, and those went even faster still. I rode motocross at a competitive level into my high school years and was accustomed to high performance machines. The car did not fit in with my sensation seeking nature, and I very quickly began looking into what could be done to improve its performance. People on the internet suggested a performance chip for the computer and a lower final drive ratio, giving the engine more mechanical advantage over the weight of the vehicle. These modifications were done without delay, but the car was still dreadfully slow. One of the worst things I have ever done to a car followed shortly thereafter, which was the removal of the original exhaust system and the installation of glass-pack mufflers. I never liked the sound, which was loud and awful to an extent beyond my ability to describe, but I had hoped to increase performance with a minimally restrictive exhaust system.
The results were not outstanding. If the car was any faster it was only by an imperceptible amount. The noise was horrendous, which reverberated and droned inside the cabin in a way that may have sounded even worse than it did to those outside the car. Not to be deterred, my attempts at finding horsepower continued. I installed a larger air flow meter, larger fuel injectors, a larger throttle body. None of this made any difference, other than to make the car less fuel efficient and less reliable. Eventually, I decided it was time to do some more substantial engine work. I found a camshaft from an M20B25 and a cylinder head from a 323i, both being different variations of this engine in a more performance-oriented state of tune. This camshaft and cylinder head were installed and the engine actually responded with an increase in power. Still, not a fast car by any means but I was moving in the right direction.
The next step forward was significant but quite difficult. The original engine management system was not calibrated to work with anything other than the standard M20B27 engine. Upon installation of the 2.5 liter cam, the engine dynamics had been changed significantly and the computer was now a significant obstacle to progress. I made a feeble attempt to explore EPROM tuning, which I had no chance of accomplishing anything with. What I needed to do was install the 2.5 liter engine management system, which meant re-wiring a harness from a later 3 series and splicing it into a 5 series engine compartment and the existing wiring around it’s periphery. Many of the sensors were different, so these needed to be changed over as well.
Not to be deterred, I began scouring through the BMW ETM. This is the electrical troubleshooting manual which contains comprehensive wiring diagrams for both the donor car and my 5 series. The main obstacle was the C101 junction at the fuse box, through which many of the critical connections were carried. About 16 wires needed to be spliced, and since the connector was a different type on the 3 series harness the e28 connector had to be carefully grafted on. Various other changes were required, mostly wiring extensions, but the work was soon completed. With the homemade wiring harness and all of the correct sensors and switches installed, the car did not start. I was disappointed, but not too surprised.
Looking back over the ETM, I checked all of my work and verified all of the connections. Everything I had done was correct, but the car did not start.
I considered this situation over the following days. Looking back over the C101 connections, I realized that there was nothing here that connects the DME to the ignition switch. This seemed like it would be necessary. How would the ignition key turn the engine off if there were no connection between the two? I looked at that section of the ETM and quickly discovered the culprit, a few wires going through a separate and not terribly important looking connector in the vicinity of the glovebox. This C104 junction carried the very important start/run signal to the computer, as well as the tachometer signal and a fuel consumption information to the instrument cluster.
A few quick splices here and the engine started immediately. The new engine management system was a vast improvement over the previous iteration. The improved idle control system was immediately apparent, and it also had advanced adaptive capabilities to adjust fueling for maximum efficiency. Best of all, the fuel and ignition mapping were suited to work with the camshaft and intake manifold I had previously installed. The car was running quite a bit better by this point, although still unacceptably loud.
The next few steps were more of the same. I installed some low quality “shorty” headers. I ordered a reground camshaft with more lift and duration. I sourced an intake manifold from a 323i on German eBay and had it shipped in. I found a chip from an Alpina C2 2.7, which was a German builder who specialized in tuning these cars. There couldn’t have been more than a few hundred of these made originally, but I found a chip out of one of those and plugged it into my DME. It provided more advanced ignition timing and a fuel map suited for a more aggressive camshaft profile.
At one point during the summer of 2006 while I was working at BMW, one of my co-workers informed me that his dental hygienist mentioned that she had an old BMW she was looking to get rid of. Vinny knew this was right up my alley, so he passed her information along and I got in touch. The car was located in a barn in Tome, NM and had been sitting for a very long time. The owner indicated that there was a problem with the alternator, but overall the car was a viable candidate. Being a 1988, it came with a number of desirable parts, including a factory installed version of the fuel injection system I had just painstakingly wired into my ’85. The price was $500, and I was shortly on my way back down to get it. The plan was to drive down in my ’85, put the good battery from my car into the ’88, the dead battery from the ’88 into the ’85, start the ’88 with the good battery and dead alternator, jump start the ’85 with the good alternator and dead battery, and drive both cars home about 45 miles before the battery in the ’88 ran down. The drive was about an hour, 45 miles distance. My buddy Brain soon discovered that the brakes didn’t work very well and nearly rolled out in front of a passing truck on highway 47. After that though, we had no issues. Both cars made it home and my second e28 project had begun.
Fortunately for myself, the neighbors, and the rest of Rio Rancho, this ‘88 had a factory dual exhaust system which was suitable for the level of horsepower I was making. Some welding was required to repair the center resonator but the system in general was solid. The glasspacks were unceremoniously shit-canned and the complete, stock ‘88 exhaust system was installed on my ‘85. The car seemed to run better than ever, while being quiet and pleasant to drive. Meanwhile, the ’88 was in the process of being comprehensively stripped down. The interior was ruined with rodent activity, so it was gutted and new carpet, seats, and dashboard parts were ordered. The engine and transmission were removed for a rebuild. This car was originally an automatic which I had no plans on retaining, so the process of converting the driveline to a manual transmission was started. This was quite easy with the engine and everything else out of the way.
At this point with the original Alpine White ’85, I had essentially reached the end of what was achievable within the limitations of this engine’s displacement and design characteristics. There were no stones left unturned, no other parts left to try. The only ways to make more power were to increase the size of the engine or spin it at higher RPM. There are practical limitations to both approaches. For the ’88, a new plan was devised using forced induction to break out of the confines of the 2.7 liter, single overhead cam architecture. Forced induction utilizes a compressor, either a belt driven supercharger or exhaust gas driven turbocharger, to supply more densely compressed air in high volume to the engine. This pushes more air mass into the existing engine and correspondingly more oxygen into the combustion chambers. Atmospheric pressure at my altitude is about 12.2 pounds per square inch. If I were to add 12.2 pounds of boost with a turbocharger, it should in theory double the amount of power the engine produces.
In practice, it doesn’t quite work out that well. The turbocharger presents a restriction in the path of exhaust gases trying to egress from the combustion chambers. This suppresses volumetric efficiency by leaving excessive residual pressure behind after the piston attempts to “blow down” the cylinder on the exhaust stroke. This residual gas remains behind in the cylinder and occupies a certain volume that cannot be filled by fresh fuel and air on the following intake stroke. If a belt driven supercharger is used, the power to drive the compressor is subtracted directly from the crankshaft. Neither approach is perfectly efficient, but both will make power.
I decided a turbocharger was the way to go. I spent countless hours reading everything available on the subject. I pored over technical information available from turbocharger manufacturers. Honeywell Garrett had an excellent website with comprehensive information regarding compressor characteristics and equations that could be used to determine what kind of air mass would be required by any given engine at any given boost level. My calculations determined that a GT2560R compressor would likely be suitable for my engine at my elevation, so I bought one, part number 466541-4. Originally, I didn’t plan on high boost levels or outrageous performance, so this turbocharger being capable of about 300 horsepower was the ideal choice.
The first problem was, how to install this device on a BMW M20 engine? This engine was never designed for turbocharging and all I have available are the various exhaust manifolds BMW manufactured for this engine. A turbocharger is generally installed close to the engine, though it can be installed practically anywhere you can fit it. They have been installed in place of rear mufflers, sticking out of hoods, inside passenger compartments, and in spare tire wells just to name a few options. I considered a rear mounted system for the sake of room, but I didn’t want to deal with feeding and returning pressurized oil to and from the back of the car. This Garrett turbo was water cooled as well, so it would also require a pair of coolant hoses running to and from where it was located. The oil return would require an electric pump, which is a potential point of failure along with the many feet of plumbing to carry these vital fluids.
After some research and consideration, I decided a conventional installation in the engine compartment was the way to go. BMW had made a diesel version of the engine with a turbocharger, and the manifold could be modified to fit the gas engine. I ordered a manifold and began work on modifying it. The manifold itself was close enough to work, only requiring a few hours of drilling, grinding and notching to fit the stud pattern on the gas engine. I found the cross-sectional area of the collector to be smaller than I liked, so I ground this out until it was significantly larger than the turbine that it fed into.
The ’85 528 was still on daily driver duty while the ’88 project progressed. By this time, it had accrued more than 314 thousand miles, the most recent of which under my ownership had seen a lifetime worth of what some might consider abuse. It was modified and making more power than ever, and being driven in a way that I’m certain it had not been accustomed to. Eventually, this would come to an end. On my way to work one morning, it began to emit a rapid, metallic, cyclical tapping noise at moderate RPM under light load. This was the sound of rod knock, which occurs when a connecting rod bearing can bear no more. The bearing had “spun” inside of the connecting rod and had opened up too great a clearance for the hydrodynamic film to carry and cushion the reciprocating load. The engine was finished. I made it to work, then back home again as carefully as possible, and the car never drove again after that.
This situation was problematic, I still had to get to work. I did have some vacation time so I used that to put in some work on the ’88. The interior had been refurbished and only the driveline remained to be addressed. I already had that engine stripped down, cleaned up, and I had parts on hand to rebuild it from a bare block. Starting with the main bearing shells, then the crankshaft, then the main bearing caps, then the rods and pistons. The front timing cover, rear main seal carrier, the oil pump and oil pan. The short block was done in an afternoon. The cylinder head had been assembled previously and was ready to install. The ’88 had a different cylinder head with larger valves and improved combustion chambers, suited to fit the hemispherical dish-in-a-dome pistons. A significant improvement over the ’85 engine, even before forced induction.
Over the course of that week, I finished assembly of the engine, installed the engine in the car, installed the transmission, driveshaft, wiring harness, reinstalled the ’88 exhaust from the deceased ’85 and got the car running before the weekend. This was a car built from a gutted, empty shell. It had its own sort of new car smell. It had a new interior, with seats I had upholstered, new carpet and new trim. The scent of the simple green I used to clean the rodent urine from the sheet metal stampings of the floor may have been faintly present. One of the last things I needed to do was bleed the brakes, which were still full of original 1988 vintage DOT 3 fluid. It was semi congealed into a lumpy, slimy broth. No wonder the brakes didn’t work.
At this point, it was on the road but not yet turbocharged. The timeline of the project had been disrupted by the untimely mechanical failure of the ’85. In any case, it was on the road and it ran beautifully. The engine was new, cylinder and valve leakage was near zero. The valvetrain was new, the camshaft was new, everything that mileage and use subjects to wear was fresh and in perfect condition. Power balance across all six cylinders was optimal. It delivered strong, smooth power over a broad range. This was a satisfactory result for the substantial work that had gone into the ’88 up to this point. With my transportation needs met, work on the turbo project continued.
I had begun to accumulate a sizable collection of spare engine parts, including a cylinder head I used to test fitment and mockup the turbo and manifold. The GT2560R used a larger compressor than BMW had fitted on the diesel engine, which would not clear the valve cover when installed. A simple but inelegant solution to this was a stack of at least seven or eight T25 flanges between the manifold and turbocharger, raising the turbo high enough to clear the cylinder head and bolt everything together. I ran this setup for probably a year and a half, having to periodically tighten the very long bolts used to hold the large stack of flanges together. Exhaust leaks were constant but with the volume of flow through the engine it had little effect on the operation of the turbocharger.
Next up was plumbing. Turbochargers draw atmosphere through a short inlet system to filter undesirable particles and deliver this under pressure through a length of plumbing. This reaches from where the turbo was located all the way to where the throttle body admits air into the intake manifold. Any self-respecting builder will certainly include an intercooler to get rid of the heat generated by the compression of the air through the turbocharger, which lengthens and further complicates the plumbing. I started with a small front mounted air to air intercooler, located below the air conditioning condenser under the front bumper. I was still considering trying to retain the functionality of the air conditioner at this point, so a certain trade off was required at the expense of intercooling.
The ’88 was now the daily driver, but I was able to begin to fabricate and assemble the plumbing in a piecemeal manner. The intercooler was installed on improvised brackets and the plumbing worked outward in both directions. The compressor outlet was on the passenger side of the engine compartment and the plumbing was constructed to feed downward and curve through the bodywork in a horseshoe shape around each side, where it connected to the intercooler in front. The throttle body was on the driver’s side, where the plumbing came up just inside the frame rail and fed into the air flow meter, which the computer uses to determine the load on the engine.
This was probably the most significant obstacle to turbocharging this engine. The turbo can supply a massive amount of air mass to the engine, however the stoichiometry of combustion requires a correspondingly large amount of fuel to be delivered to maintain an appropriate air/fuel ratio. The fuel injection system was never designed to work with anything other than atmosphere, so this required some engineering. At the time in 2006, options were limited. The best solution at the time was a rising rate fuel pressure regulator. This simple device references fuel pressure to boost pressure, and scales up fuel pressure at an adjustable rate of gain to deliver enrichment under boost. The computer does not see the boost or any change in load and the engine still displaces 2.7 liters. The RRFPR simply overrides the standard fuel pressure regulator when boost pressure is generated. The computer fires the fuel injectors for the exact same duration that it would ordinarily, but with the increased fuel pressure additional fuel is delivered.
This completely resolves the enrichment issue, but doesn’t completely address the obstacle posed by the fuel injection system. The other factor must be addressed is ignition timing, which is advanced at lower loads and pulled back at higher loads. The original computer handles this assuming maximum load is at atmospheric pressure. With forced induction, maximum load is determined by the maximum boost pressure and ignition timing should be scaled downward further as boost increases. If the air fuel ratio or ignition timing is not carefully adjusted, abnormal combustion occurs known as “detonation” which is a spontaneous, powerful and rapid ignition of mixture inside the combustion chamber. This phenomenon is very destructive and is the most common cause of engine damage in high performance engines, especially those using forced induction.
Fortunately in a way, and unbeknownst to me at the time, my intercooler was significantly undersized. It was unable to control charge air temperatures effectively, so the air flow meter was seeing significantly elevated air intake temperatures. The original computer responds to this by pulling back ignition timing to avoid detonation, which is exactly what was needed to save my bacon. I’m not sure to what extent this was beneficial overall, as these same elevated air intake temperatures contribute to detonation as this heat enters the combustion chamber and exacerbates the adiabatic heating that occurs during the compression stroke.
In any case, with the fuel enrichment handled and a certain amount of indifference toward my inability to address ignition timing, I moved on with the project. The turbocharger and exhaust manifold were ready, I had flanges, bends and tubing to fabricate a new exhaust system. I had the intake plumbing essentially competed. I had routed coolant from the original throttle body heater circuit to the turbocharger. I tapped into the clean, pressurized supply of oil available at the oil cooler adapter and installed a fitting here to supply the turbocharger. The oil return was plugged haphazardly into the oil pan and sealed with the finest quality high strength, steel reinforced epoxy.
In spring 2007, the ’88 was ready for boost. The installation did not require vacation time as all of the loose ends and potential hang-ups had been sorted out in advance. The manifold had been test fitted, the plumbing had been fabricated and was already almost completely installed before I installed the business end of the system. I would still need to sort out the rate of gain on the RRFPR to dial in the fueling, but this was a simple device with few adjustments. Cautiously at first, the original turbo 528e hit the road. The tuning was simple enough, I had previously spent many hours adjusting carburetors on the dirt bikes to fine tune fuel mixtures. This experience translated well to the turbo car. I started with excessively rich, or fuel heavy air fuel mixtures. As I leaned the mixture out, the car stopped breaking up and misfiring and began making what felt like a ridiculous amount of horsepower.
At that boost level, I would estimate the car was making about 200 rear wheel horsepower. At the crank, close to 240. This car was quick even at 7 psi. For this altitude, anything without a turbo on it is paying a roughly 20% penalty with the reduced air density. A stock LS1 in a Camaro SS or Trans AM WS6 was making 300 horsepower at the crank, at sea level. In Rio Rancho at the rear wheels? Maybe 205. I recall a specific instance where I lined up with one of those LS-equipped Pontiacs, and we both opened it up when the light turned green. Though both cars were accelerating rapidly, we were completely stationary relative to one another. Despite the vastly different powertrains and 20+ year difference between these cars, the different gear ratios and torque curves, we were accelerating at exactly the same rate. I think we let off at about 100, which was fortunate as there was a police officer sitting in a Target parking lot off to the side, perhaps another quarter mile down the road. We would have been going more than triple the posted limit by that point, and doing so while street racing. That could have been a bad night, but was the first of many such close calls.
I would have loved to talk to the guy in the Pontiac. I couldn’t believe I hung with a car like that, and I’m sure they were just as surprised as I was. This was the most awesome thing about that e28. Dragged out of a barn, covered in rodent excrement. Resurrected, at least mechanically, and modified to produce enough power to stand toe to toe with the latest iteration of GM’s high performance 5.7 liter V8. Though the interior was nice, the paint and body on the ’88 was not on the same level as the ’85. Even when new, it was painted a butt-ugly metallic brown. Nerzbraun, if I remember correctly, which translates to “Mink Brown”. The paint was faded and the clear coat had begun to peel, so it wasn’t much to look at in 2007. Worst of all, the car had been hit and damaged in a rear end accident shortly after it was returned to the road. The damage had affected the right rear quarter panel and broken the rear bumper in half. This pissed me off severely but it didn’t look too bad once I had replaced the taillight. The car had been paid out as a total loss, so I had more money for turbo parts. This disguise added to the shock and dismay of it’s victims. You would never see it coming, and it was a serious contender.
Shortly after the system was completed, the ’88 went to the dragstrip for a sort of performance evaluation. This provides a substantive basis for comparison, the sum of all factors. Some aspect of this is left to the ability of the driver but for the most part, the quarter mile run provides a very good test. Launching this car was difficult, even with relatively mild amounts of horsepower. This was the furthest thing from this vehicle’s intended purpose, and the power output of the original engine had been more than doubled. Despite uniformly poor results in the first 60 feet, during the period between not moving and moving, the car covered the distance in very close to 14 seconds flat. Better launches and a lower 60 foot time would have provided better ET’s, but a 14 flat is nothing to sneeze at. Trap speeds were around 100 miles an hour, which roughly corresponds to the elapsed time.
The thrill and euphoria of these things is unfortunately short lived. Given a few weeks of excitement, the newfound performance became familiar and increasingly ordinary. Still a young man, always looking for more, I began exploring the possibility of turning the boost up beyond the original .5 bar allowed by the wastegate actuator. The system was already marginal in many ways, and I bumped against these limitations as soon as I tried to push more boost. The original computer knew nothing of the hot rod shenanigans that it was involved with, and was increasingly unsuitable for boost as it crept higher. I found a custom chip with moderated ignition timing through Todd at TCD, a supplier who had recently brought legitimate turbo systems to market for e28’s. This got me to 11 psi, which made the car go faster still. I had to resort to zip ties and duct tape between the air flow meter and throttle body though, as the original rubber boot was never designed to hold even a strong vacuum, let alone 11 pounds of boost. Fuel pressure was reaching levels more than double what the system was intended to run, which was soon going to require more fundamental changes.
This was about when the car went to the dyno for the first time. Quoting myself from forum posts of the period, I was running 11 psi and the car made 230 rear wheel horsepower and 266 foot-pounds of torque. This would perform comparably to a contemporary BMW M3, whose S54B32 engine produced 333 horsepower. At my elevation, 333 crank horsepower translates to 227 at the wheels. And my e28 was lighter. My only gripe at the time was the relative lack of top end power, the dyno curve began to drop excessively as revs passed 5500 RPM. Peak horsepower was lower than would be expected for this engine configuration, so something was suppressing the last third of the power curve. In hindsight, I think this can be attributed to the insufficient intercooling and rapidly climbing intake air temps. Not only does this elevate the probability of detonation, the hot boost is less dense than it could be, as the overall air mass delivered for a given volume of air is reduced.
I think the highest I ever went with the original system was 14 psi, and this was more than the original clutch could handle. I had to turn it back down immediately and start shopping for a stronger clutch. Todd at TCD had a solution for me for a few hundred dollars. This was an organic disc with a special pressure plate designed to generate lots of clamping force. Designed to hold almost 400 foot-pounds of torque. That seemed sufficient for any prospective boost levels, so I ordered one up.
The next step for power was a bigger turbo and standalone fuel injection. I was not at all concerned about a bigger turbocharger, this is a bolt on affair. My hypothesis was that the GT2560R was restrictive on the turbine side, which presents a choke point for the exhaust gases on their way out from the combustion chamber. Every pound of air that goes through the engine has to squeeze through this opening in the turbine housing that was approximately the size of a large grape. 230 rear wheel horsepower requires about 23 pounds of air per minute, which is a lot of air. A larger turbine would trade off some of the response and raise the boost threshold, which is the RPM which the turbo fully spools and makes significant boost. Regardless, this was the next step, so the turbo was ordered, a Garrett GT2871R .86, part number 472560-15. Part of the appeal of the GT2560R was that it shared almost all of it’s design features with a family of other turbochargers. Garrett described these as “outline interchangeable”, meaning I could bolt on a larger unit without having to weld on new flanges or change plumbing.
The real battle was shaping up for fuel injection. My ability to work around the limitations of Bosch Motronic was at its end. I had done all I could but it was simply no longer possible to make any more power without an unacceptable risk of engine damage. The solution was a product called Megasquirt, a standalone computer that replaces the original engine management computer and offers full control over every parameter of the engine’s operation. Tuning can be performed while you drive with a laptop computer. This sounds great, but it also means that you are responsible for configuring and tuning every single parameter of the engine’s operation. I wanted more power though, so I found a guy in the e28 community who was building these MS2 kits into the original Bosch Motronic boxes. This allows a plug and play functionality, which retained the ability to plug the original computer back in if need arose and I had to get the car home.
At the time, this was the most significant challenge of the project. This was far above and beyond fabrication and designing a layout. I had read a great deal about tuning, and I had a lot of experience with carbs on two stroke engines. I had no experience building three dimensional maps for fuel and ignition timing though, let alone tuning acceleration enrichments, cranking pulsewidth, configuring ignition settings or any of the other 100+ variables that I was now trying to sort out. It could be compared to teaching someone how to put on shoes, stand up, walk, run, jump, then compete at an Olympic level. This is a process that stretches into the hundreds of hours.
The good news in that the car did eventually get going on standalone, and the new turbo did make more power. Standalone injection offered many advantages once the initial period of configuration hell had been successfully navigated. I now had the ability to record datalogs containing a record of every sensor input and every output by the standalone computer. I had shortly discovered how severely undersized my intercooler was by observing the intake air temperature under boost. It climbed as rapidly as RPM, reaching levels that would rapidly defrost a breakfast sandwich. I immediately ordered another intercooler to install in series with the original. The internet said it couldn’t be done, that pressure drop would be too great and it would be horribly inefficient. I did it anyway. Pressure drop was not significantly greater than it was with the single front mounted intercooler and the intake air temps were within twenty degrees of ambient. A significant improvement in both performance and reliability.
The next trip to the dragstrip was later that summer. On this night, with more boost provided by the larger turbocharger and supported by the standalone fuel injection, the car was running 13 second quarter mile times at 108 miles an hour. Launching was still not great, and this was the only thing holding the car back from breaking into the 12 second category. I had to settle for a best ET of 13.01 at 108 miles an hour. The car got off the line better on the street. The surface at the dragstrip was a nearly smooth type of pavement with a coating of rubber laid down on top. With the right type of tire, this generates enough traction to destroy driveline parts and tear subframe and differential mounts right out of the unibody. With the type of tires I was running, I could only produce wheelspin at best. I rarely drove at the dragstrip and drag radials would almost certainly require a substantial reinforcement of the rear suspension, so this was fine with me.
The next trip to the dyno was in the fall of 2007, and the car made 300 rear wheel horsepower and 360 foot-pounds of torque. Would compare well on the streets of Albuquerque to a non-turbo engine that makes 450 crank horsepower at sea level. It did in fact compare well to a stock BMW 335i, the new twin turbo 3 series introduced in 2007. Another member of a local car forum had one of those and was left behind by bus-lengths while going head to head with the e28. Video of this evening still exists in the hallowed halls of YouTube. That was a fun night, and I engaged in this sort of high risk activity on a frequent basis.
One instance in which I wasn’t so lucky occurred on a lunch break, likely on my way to Arby’s for a three for five deal. I had come down Second Street and gotten on eastbound Paseo Del Norte, and seeing a clear road ahead for at least a half mile I put the hammer down. The turbo spooled up in third gear and the traffic that was once close behind diminished to distant specks in the rearview mirror. I had not checked my mirrors closely enough though, as there was a Bernalillo County Sherriff among that group of cars. Third gear would hit 120 and I’m pretty sure it did before I began coasting down toward Jefferson. About the time I got off the power, I observed the red and blue lights catching up from behind, and I pulled over on Jefferson for what was certain to be an unpleasant experience.